OK, well it’s back to work on the broken Jetta. I just can’t afford to drive this truck everywhere I need to go! I went back to Portland a few days ago, and spent another pile of cash on more parts. Aren’t they purty?
That’s about $720 sitting there!
Anyway, on to the task at hand. We left off with the head removed and marveling at the damage. The next job is to scrub the top of the block and the bolt holes clean, and get the head ready to install. Manifolds go back on now, and new glow plugs. Another task that you won’t find in the Bentley manual is peening the head around the pre combustion chambers. These little inserts are common to many indirect injection (IDI) diesel engines and have been known to work themselves loose and fall out of aluminum heads like this one. So a few strokes with a punch and a hammer are needed to deform the soft aluminum around the inserts and help keep them from coming loose. Careful not to peen where the sealing edge of the gasket sits! That’s what the little arcs in pen are for: to remind me of where that edge will be. Thanks to the guys at dieselvwparts forums for making me aware of this potential trouble spot.
Here’s a picture:
Make sure that none of the pistons are at the top of their stroke when you set the head down, so you don’t damage a valve. These diesel heads have next to no room to spare for a valve being open in the wrong place. After some futzing around and improvising to hold the gasket in place, I set the head down and started the bolts in finger tight to hold it in place. This is an awkward job if you are alone like I was. Careful of your back, that thing is heavy with the manifolds on. Next thing is to lightly oil the bolts around the washers, cross your fingers and torque the head to the Bentley manual specs. These are Torque to Yield (TTY) bolts and can only be tightened once.
At this point, I had to switch programs to deal with some tedious tasks: changing the water pump and the intermediate shaft seal. None of this part was very fun, and I was too distracted to remember to take any pix. I had to make a special tool to hold the IM shaft pulley while I removed the bolt. Here is version 2 of that tool; version 1 was partly made of flat stock instead of angle iron and it bent all to heck when I leaned into it. I sure love having a cutting torch around. I know this isn’t as pretty as one made with a bandsaw and a drill press would have been, but the torch is fast.
I lucked out on the water pump; often the bolts just break off in the aluminum housing, leaving you with a really annoying removal job or another trip to town for a new housing. Fortunately for me, someone had already changed the water pump once before, and all the bolts came out easily and without breaking.
So, at the end of the workday today, I have the head installed and torqued down, the water pump, thermostat and IM shaft seal all replaced with new ones, and I am ready to install the timing belt and rebuild the injectors. Stay tuned!
Tomorrow, though, is a kayaking day.